South East Scoobies  

Go Back   South East Scoobies > The Garage > Engine Management

Engine Management For all your mapping,diagnostics and electronics

Reply
 
Thread Tools
  #1  
Old 18-05-2013, 09:03 PM
bonner's Avatar
bonner bonner is offline
Silver Member
 
Join Date: Nov 2012
Location: East sussex
Posts: 1,288
Default lost boost?

hi all been working local and not used the motor properly for a good month, got back from mexico and battery was almost dead luckily she fired up, thought Id give it a good blast once wam and boost was only reaching 0.5 bar! usually a notch under 1 bar of boost, I found it would reach higher a
near redline but this is not right, usally boost gauge will instanly show just under a bar when boosting, other than that it drives fine with no issues
__________________
Reply With Quote
  #2  
Old 18-05-2013, 09:09 PM
Mortster's Avatar
Mortster Mortster is offline
Gold Member
 
Join Date: Apr 2009
Location: Milford, Surrey
Posts: 2,432
Default

Check all the boost hoses, the ones above/near can get brittle and split.
__________________
2001 Bugeye - Project Black/Red, 1997 JDM Type R, 1995 V1 WRX, Defender Tithonus MOD Styleeee!
Reply With Quote
  #3  
Old 18-05-2013, 09:11 PM
bonner's Avatar
bonner bonner is offline
Silver Member
 
Join Date: Nov 2012
Location: East sussex
Posts: 1,288
Default

Quote:
Originally Posted by Mortster View Post
Check all the boost hoses, the ones above/near can get brittle and split.
il have a buchers mate but I replaced them all for silicone. wondered if the actuator might need lubeing but cant see it need doin
__________________
Reply With Quote
  #4  
Old 18-05-2013, 11:25 PM
riiidaa riiidaa is offline
Rest in peace Jodie.
 
Join Date: Mar 2009
Location: Wallington
Posts: 1,407
Default

Restrictor pill?
Reply With Quote
  #5  
Old 18-05-2013, 11:38 PM
555_Si's Avatar
555_Si 555_Si is offline
Moderator
 
Join Date: Aug 2012
Location: Horsham
Posts: 2,236
Default

my actuator became sticky recently, went from 1 bar to .7 then finally to nothing.

Freed it up and it was back to normal, you can put a large syringe on the pipe going to it and see if it moves.
__________________
2002 Bugeye WRX Wagon - deceased
1995 555 STi v2 track build
1999 RB5
2003 Blobeye WRX SL Wagon
Reply With Quote
  #6  
Old 19-05-2013, 02:14 AM
bonner's Avatar
bonner bonner is offline
Silver Member
 
Join Date: Nov 2012
Location: East sussex
Posts: 1,288
Default

Quote:
Originally Posted by Wagon_Si View Post
my actuator became sticky recently, went from 1 bar to .7 then finally to nothing.

Freed it up and it was back to normal, you can put a large syringe on the pipe going to it and see if it moves.
il have bash mate was fine till I got back, strange
__________________
Reply With Quote
  #7  
Old 19-05-2013, 08:22 AM
Scott.T's Avatar
Scott.T Scott.T is offline
Admin, Meets/Events Organiser.... formerly known as SilverSurfer
 
Join Date: Sep 2008
Location: Hastings, East Sussex
Posts: 9,485
Default

Quote:
Originally Posted by riiidaa View Post
Restrictor pill?
Yep......that'll be the problem if the hoses have been replaced for silicon.
The short hose from the turbo outlet nipple to the t-piece has a brass restrictor inside.
If you have swapped this for silicon and not fitted the restrictor then the actuator will be seeing the incorrect level of boost and opening too early.
Reply With Quote
  #8  
Old 19-05-2013, 12:19 PM
bonner's Avatar
bonner bonner is offline
Silver Member
 
Join Date: Nov 2012
Location: East sussex
Posts: 1,288
Default

Quote:
Originally Posted by SilverSurfer View Post
Yep......that'll be the problem if the hoses have been replaced for silicon.
The short hose from the turbo outlet nipple to the t-piece has a brass restrictor inside.
If you have swapped this for silicon and not fitted the restrictor then the actuator will be seeing the incorrect level of boost and opening too early.
the only ones I didnt change were on the turbo as I ran out but car has been boostin fine up till now? only since its been sitting, will give it all a good going over later and see if anythings loose
__________________
Reply With Quote
  #9  
Old 24-05-2013, 10:48 AM
bonner's Avatar
bonner bonner is offline
Silver Member
 
Join Date: Nov 2012
Location: East sussex
Posts: 1,288
Default

Hi all how can i reset my ecu without causing any issues with reprogramming the key? cheers
__________________
Reply With Quote
  #10  
Old 24-05-2013, 12:07 PM
Anger's Avatar
Anger Anger is offline
Platinum Member
 
Join Date: Oct 2008
Location: Bletchingley Surrey
Posts: 4,973
Default

Should be fine
__________________
"We're here for a good time, not a long time...." Colin McRae MBE 1968-2007
Reply With Quote
  #11  
Old 24-05-2013, 12:34 PM
bonner's Avatar
bonner bonner is offline
Silver Member
 
Join Date: Nov 2012
Location: East sussex
Posts: 1,288
Default

Is it just the case of disconecting the battery?
__________________
Reply With Quote
  #12  
Old 24-05-2013, 01:07 PM
SpecB's Avatar
SpecB SpecB is offline
Moderator (formerly known as Bluebugeye!)
 
Join Date: Mar 2009
Location: Littlehampton
Posts: 4,345
Default

Not sure exactly but it involves the test plugs under the dash I think
__________________
2005 Spec B 6MT - KiDO tuned (~270Bhp)
Custom exhaust - Cosworth filter - Samco Intake - Tints - Bilstein B8/B6 & STI springs - SuperPro ALK - Whiteline positive shift kit, rack mounts, rear adjustable camber bushes, front ARB mounts & strut brace, 20mm rear ARB with AVO mounts, - Hardrace Gearbox and pitch mounts - Prodrive PFF7's - Front Brembos - Kenwood CarPlay - 1/2 carbon grille - STI front splitter
Reply With Quote
  #13  
Old 24-05-2013, 01:44 PM
bonner's Avatar
bonner bonner is offline
Silver Member
 
Join Date: Nov 2012
Location: East sussex
Posts: 1,288
Default

I did read about these plugs but i assumed it was classic only, also pushing the brake pedal but didnt read on for that reason, just curious as im testing the actuator tomorrow and if it works fine then plan b the reset, if that dont work il look at changing turbo pipes, cheers
__________________
Reply With Quote
  #14  
Old 25-05-2013, 03:10 AM
bonner's Avatar
bonner bonner is offline
Silver Member
 
Join Date: Nov 2012
Location: East sussex
Posts: 1,288
Default

Thanks for your input guys! battary was seriously low so just took out for a blast on the bypass to find my boost has magicly come back?.strange! could have been down to what si suggested a sticky actuator due to notvbeing used for a month or so, hopfully all sorted still goin to give a good nose over thanks again!
__________________
Reply With Quote
Reply


Currently Active Users Viewing This Thread: 1 (0 members and 1 guests)
 



All times are GMT +1. The time now is 06:22 AM.


Powered by vBulletin® Version 3.8.11
Copyright ©2000 - 2024, vBulletin Solutions Inc.

Opinions expressed are not necessarily the opinions of SouthEastScoobies or any individuals directly or indirectly involved in this website. No responsibility is taken or assumed for any comments or statements made on this or any associated website. Visitors who use this website and rely on, or act on any information do so at their own judgement, discretion and or risk. SouthEastScoobies or its content providers shall not be liable for any loss or damage arising from or otherwise in connection with your use of SouthEastScoobies forums. It is not possible for the Administrators of these forums, or the Moderators participating, to fully and effectively monitor Messages that are submitted for infringement of third party rights. If you believe that any information within the forums infringes your legal rights, or gives cause for concern you should notify an Administrator or a Moderator immediately giving such information to enable the recipient to amend, delete or remove in its entirety the message, at their earliest convenience.