South East Scoobies  

Go Back   South East Scoobies > The Garage > General Mechanics

Reply
 
Thread Tools
  #1  
Old 25-02-2013, 07:12 PM
Bugeye-Steve's Avatar
Bugeye-Steve Bugeye-Steve is offline
Regular User
 
Join Date: Jun 2012
Location: Strood
Posts: 22
Default Idle and rev problem :-(

Hi not been on in a while
I have a 51 plate bug eye over the last few weeks i got stuck in stop start traffic now its been idling funny like ticking over at around 500rpm and sometimes drops right down to nearly 0 I have no engine lights on either . Was told try new plugs and fuel filter but no different (HELP PLEASE ) .
Reply With Quote
  #2  
Old 25-02-2013, 07:16 PM
SpecB's Avatar
SpecB SpecB is offline
Moderator (formerly known as Bluebugeye!)
 
Join Date: Mar 2009
Location: Littlehampton
Posts: 4,345
Default

Possibly the MAF needs a clean, is it remapped at all?

Also the ISV could be gummed up.
__________________
2005 Spec B 6MT - KiDO tuned (~270Bhp)
Custom exhaust - Cosworth filter - Samco Intake - Tints - Bilstein B8/B6 & STI springs - SuperPro ALK - Whiteline positive shift kit, rack mounts, rear adjustable camber bushes, front ARB mounts & strut brace, 20mm rear ARB with AVO mounts, - Hardrace Gearbox and pitch mounts - Prodrive PFF7's - Front Brembos - Kenwood CarPlay - 1/2 carbon grille - STI front splitter
Reply With Quote
  #3  
Old 25-02-2013, 07:17 PM
SamSTI's Avatar
SamSTI SamSTI is offline
Silver Member
 
Join Date: Aug 2012
Location: Seaford
Posts: 1,214
Default

I had this problem on my last scooby (blob wrx), I cleaned the idle control valve which cured the problem.

Hope this helps
Reply With Quote
  #4  
Old 25-02-2013, 07:20 PM
C. J.'s Avatar
C. J. C. J. is offline
Platinum Member
 
Join Date: Sep 2008
Location: Horsham
Posts: 5,081
Default

sounds like ICV
Either delete the water passage going through the throttle body which isnt need here as it dont get cold enough or by a new gasket before taking apart

Last edited by C. J.; 25-02-2013 at 07:22 PM.
Reply With Quote
  #5  
Old 25-02-2013, 07:21 PM
Bugeye-Steve's Avatar
Bugeye-Steve Bugeye-Steve is offline
Regular User
 
Join Date: Jun 2012
Location: Strood
Posts: 22
Default

Not yet was told it might run poor as its had a walbro pump /up pipe / and a new k&n filter on a standard ecu . Will try clean them out tomora shall I just use like a carb cleaner spray ??
Reply With Quote
  #6  
Old 25-02-2013, 07:23 PM
C. J.'s Avatar
C. J. C. J. is offline
Platinum Member
 
Join Date: Sep 2008
Location: Horsham
Posts: 5,081
Default

Quote:
Originally Posted by Bugeye-Steve View Post
Not yet was told it might run poor as its had a walbro pump /up pipe / and a new k&n filter on a standard ecu . Will try clean them out tomora shall I just use like a carb cleaner spray ??
yes and sock it for a while if poss
Reply With Quote
  #7  
Old 25-02-2013, 07:29 PM
Bugeye-Steve's Avatar
Bugeye-Steve Bugeye-Steve is offline
Regular User
 
Join Date: Jun 2012
Location: Strood
Posts: 22
Default

Ahh cheers guys will let u no how I get on once cleaned if not il replace . Now have engine light on being a dick I unplugged the icv with engine running n light stayed on . Luck next door has a snap on code reader . Just thought could a dodgy hks bov cause this ??
Reply With Quote
  #8  
Old 25-02-2013, 07:42 PM
majorscooby majorscooby is offline
Platinum Member
 
Join Date: Dec 2008
Location: gravesend, kent
Posts: 3,298
Default

Hmmm, sounds interesting. I have recently put a walbro 255 on mine and its running really poo, everything standard on my car, but revs hunting and dropping down to zero when approaching traffic lights as I dip the clutch to stop. Never did it with the standard one.I've been pointed in the direction of my MAF which is a poss as its 13 years old but your the third person that has a walbro on then had issues???
As for the BoV I had a similar prob with my Forge one. Each time I stopped and dipped the clutch pedal the revs fell and the car nearly stalled, took it off put the original recirc back on and the problem went away.
__________________
Cooper man!!!!!
Reply With Quote
  #9  
Old 25-02-2013, 07:55 PM
Bugeye-Steve's Avatar
Bugeye-Steve Bugeye-Steve is offline
Regular User
 
Join Date: Jun 2012
Location: Strood
Posts: 22
Default

Yeah the hks bov somtimes don't dump like its ment to . As for the pump now been told walbro use a smaller sock reducing the flow more than a standard ?? Gonna clean the icv and see then if not may just drop it into slowboy racing cheers for help and comment tho
Reply With Quote
  #10  
Old 25-02-2013, 08:26 PM
majorscooby majorscooby is offline
Platinum Member
 
Join Date: Dec 2008
Location: gravesend, kent
Posts: 3,298
Default

Quote:
Originally Posted by Bugeye-Steve View Post
Yeah the hks bov somtimes don't dump like its ment to . As for the pump now been told walbro use a smaller sock reducing the flow more than a standard ?? Gonna clean the icv and see then if not may just drop it into slowboy racing cheers for help and comment tho
Yeah I've heard about the pre filter issue being smaller which it is as I noticed when changing mine. I used the original larger sock.
__________________
Cooper man!!!!!
Reply With Quote
  #11  
Old 25-02-2013, 09:56 PM
Type-r-russ's Avatar
Type-r-russ Type-r-russ is offline
Silver Member
 
Join Date: Jun 2011
Location: Eastbourne
Posts: 604
Default

Quote:
Originally Posted by C. J. View Post
sounds like ICV
Either delete the water passage going through the throttle body which isnt need here as it dont get cold enough or by a new gasket before taking apart
mine idles a bit lumpy its been mapped for no maf do you think this could be ICV
Reply With Quote
  #12  
Old 25-02-2013, 10:56 PM
bonner's Avatar
bonner bonner is offline
Silver Member
 
Join Date: Nov 2012
Location: East sussex
Posts: 1,288
Default

Quote:
Originally Posted by Bugeye-Steve View Post
Ahh cheers guys will let u no how I get on once cleaned if not il replace . Now have engine light on being a dick I unplugged the icv with engine running n light stayed on . Luck next door has a snap on code reader . Just thought could a dodgy hks bov cause this ??
as major says try the original recurc!! my blobeye ran perfect when i first got it! i also have a supposidly hks black limited this was the first thing i changed and once fitted and fired up it ran lumpy almost cutting out! i have the same problem myself worse in the mornings from cold! also where did you get the hks from? there are many fakes about with mine being one of them! google it as there is a thread on s,net showing detailed images and what to look for! the first thing is the hks stamp on the back! should be like a silver crest and the lettering hks in hologram!!

alot have said about the icv so try both!
__________________
Reply With Quote
  #13  
Old 25-02-2013, 11:10 PM
Bugeye-Steve's Avatar
Bugeye-Steve Bugeye-Steve is offline
Regular User
 
Join Date: Jun 2012
Location: Strood
Posts: 22
Default

I have a receipt for it from scooby world . Yeah a few mates have had a few wrong uns . Yeah gonna try again tomora hopefully will get it sorted . Another question can the ecu be reset by hand or only a computer ?
Reply With Quote
  #14  
Old 26-02-2013, 07:28 AM
SpecB's Avatar
SpecB SpecB is offline
Moderator (formerly known as Bluebugeye!)
 
Join Date: Mar 2009
Location: Littlehampton
Posts: 4,345
Default

You can reset by hand using the test connectors under the dash, I think JGM has instructions on his site.

If you clean the ISV make sure you get a new gasket first as you'll never get the old one back in!
__________________
2005 Spec B 6MT - KiDO tuned (~270Bhp)
Custom exhaust - Cosworth filter - Samco Intake - Tints - Bilstein B8/B6 & STI springs - SuperPro ALK - Whiteline positive shift kit, rack mounts, rear adjustable camber bushes, front ARB mounts & strut brace, 20mm rear ARB with AVO mounts, - Hardrace Gearbox and pitch mounts - Prodrive PFF7's - Front Brembos - Kenwood CarPlay - 1/2 carbon grille - STI front splitter
Reply With Quote
  #15  
Old 26-02-2013, 06:57 PM
Bugeye-Steve's Avatar
Bugeye-Steve Bugeye-Steve is offline
Regular User
 
Join Date: Jun 2012
Location: Strood
Posts: 22
Default

Afternoon guys just have the bug eye code read again after trying to clean the icv but with no luck . Again no faults found he seems to think i have a air leak somewhere are there any common pipes that go ? Its still hitting around a bar of boost tho with no problems ?
Reply With Quote
  #16  
Old 05-03-2013, 06:36 PM
Bugeye-Steve's Avatar
Bugeye-Steve Bugeye-Steve is offline
Regular User
 
Join Date: Jun 2012
Location: Strood
Posts: 22
Default

Sorry lads only me again . There is a electronic valve ? On the passenger side of the engine beside the washer bottle with around a 3 inch hose coming of it . Dose anyone no what this is or weather it's meant to be connected to anything??
Reply With Quote
Reply


Currently Active Users Viewing This Thread: 1 (0 members and 1 guests)
 



All times are GMT +1. The time now is 11:16 AM.


Powered by vBulletin® Version 3.8.11
Copyright ©2000 - 2024, vBulletin Solutions Inc.

Opinions expressed are not necessarily the opinions of SouthEastScoobies or any individuals directly or indirectly involved in this website. No responsibility is taken or assumed for any comments or statements made on this or any associated website. Visitors who use this website and rely on, or act on any information do so at their own judgement, discretion and or risk. SouthEastScoobies or its content providers shall not be liable for any loss or damage arising from or otherwise in connection with your use of SouthEastScoobies forums. It is not possible for the Administrators of these forums, or the Moderators participating, to fully and effectively monitor Messages that are submitted for infringement of third party rights. If you believe that any information within the forums infringes your legal rights, or gives cause for concern you should notify an Administrator or a Moderator immediately giving such information to enable the recipient to amend, delete or remove in its entirety the message, at their earliest convenience.